Motor mounted, chain shortend and tensioned, test run performed.
It will gladly rev the tyres on a stand, but will judder/do heavy cogging when trying to start from a stand still. Unsure what next move is. Better gearing would be nice, the Brushless controller i have on the RC car won’t do much higher voltage, maybe just time to shell out for a proper DC motor?
Seating position is a wee bit sketchy too, but it’s fiiiine.
Per a side note, my welding is getting somewhat better, especially the ones not made to the thin frame parts.